Thu, 17 Oct 2019 00:13:50 +0200
new post on the eip545b fw
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[tek] part 2 of the PSU repair
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1 | ========================================== |
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[tek] part 2 of the PSU repair
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2 | Tektronics 2445 scope PSU repair: part 2 |
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3 | ========================================== |
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4 | |
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5 | :Author: David Douard |
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6 | :Category: Electronics |
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7 | :Tags: Tektronics, 2445, analog scope, repair, test equipment |
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8 | :series: Tek2445 PSU repair |
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9 | :series_index: 2 |
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10 | |
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11 | After a `quick repair of the PSU of my Tek 2445 |
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12 | <{static}/TeK2445.rst>`_, I've started a more systematic replacement |
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13 | of the capacitors. |
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14 | |
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15 | .. image:: {static}/images/tek2445/psu_caps_replaced.jpg |
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16 | :alt: Tek2445 PSU Caps being replaced. |
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17 | |
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18 | But I was also a bit worried because of a dirty noise coming from the |
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19 | preregulator area. |
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20 | |
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21 | After having replaced most of the electrolytic capacitors, the dirty |
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22 | noise became louder (I think. It might be unrelated, not sure |
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23 | yet). The PSU became very untrusty: a small plume of smoke began to |
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24 | escape from somewhere (could not identify precisely where exactly). I |
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25 | started probing around, but at this moment, I had no idea which |
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26 | component was getting too hot: I always shut the power off after a few |
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27 | seconds of power, with the T1050 transformer singing as soon as the |
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28 | preregulator control oscillator starts up (U1030). |
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29 | |
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30 | During this probing and checking period, I discovered that the CR1040 |
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31 | diode from the current limitation circuit was dead |
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32 | (short)... Unfortunately, it's a germanium diode (used for it's low |
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33 | voltage drop, about 0.2v). Fortunately I found one of them which |
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34 | should fit in my very old spare components casket (the one I had when |
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35 | I was a kid). |
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36 | |
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37 | Then, in order to try to see things, I started to power the PSU up for |
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38 | a few seconds (sometimes maybe tens of seconds) trying to probe |
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39 | (without my scope, obviously, so only with my Fluke 867B which allows |
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40 | me to see *some kind* of signals.) |
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41 | |
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42 | Which allowed me to finally find the culprit for the smoke: R1071 (in |
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43 | red on the schematic below). Its value is still fine, but it's getting |
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44 | very hot as soon as the main oscillator starts up. A bit strange, |
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45 | since the capacitor C1071 seems fine (I do not have a ESR meter, but |
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46 | hey, there is no way higher ESR could lead to overcurrent flowing |
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47 | through this resistor). |
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48 | |
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49 | .. image:: {static}/images/tek2445/psu_prereg.png |
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50 | :alt: Schematic of the preregulator of teh Tek2445 |
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51 | |
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52 | But powering up and down the PSU again and again, with its freaking |
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53 | and noisy switching problem, finally killed the MOSFET (IRF820) power |
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54 | transistors (Q1050, Q1060 and Q1070) producing flames. The plastic |
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55 | protection on Q1060 directed all the heat directly on the poor LR1060 |
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56 | which exploded as well... Which is a problem since I do not know the |
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57 | exact specifications of the device; the service manual do not give the |
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58 | value of the resistor in parallel with the 2.5µH inductance. |
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59 | |
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60 | .. image:: {static}/images/tek2445/dead_transistors.jpg |
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61 | :alt: Q1050, 1060 and Q1070 are dead. |
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62 | |
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63 | For now, I've picked up a 3W 100Ω resistor and I've made a self by |
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64 | hand. As I don't have a RLC meter, I don't known its exact value so |
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65 | I've took a few measures of its impedance at several frequencies, and |
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66 | I estimate the inductance to be around 4 µH. I have no idea whether |
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67 | this higher value might be a problem... But I've no idea either if the |
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68 | 100Ω resistor I've used as core for the coil is fine or not. |
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69 | |
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70 | And I have other problems to fix. First, the 3 MOSFETs have to be |
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71 | replaced... As I don't have anything near IRP820 in my hood, I've |
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72 | picked up some IRFP450 I extracted from computer PSUs. These are much |
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73 | bigger than the IRF820, but having beafier models (with higher max |
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74 | current and voltage) should not be a problem there. The only thing |
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75 | that worries me a bit is the much lower Rds value (0.4Ω versus 3Ω for |
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76 | the IRF820). Means higher peak currents. Q1030 and R1052 also |
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77 | died. The transistor is a 2N3905 (which I don't have around either) so |
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78 | I've replaced it with a bigger TIP32C. |
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79 | |
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80 | .. image:: {static}/images/tek2445/beafier_transistors.jpg |
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81 | :alt: Beafier replacement rtansistors, and a handmade coil. |
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82 | |
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83 | From there, I began to check most of the components in this |
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84 | preregulator part of the PSU before even attempting to apply power. |
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85 | |
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86 | I've checked the behavior of the main control oscillator (made |
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87 | of U1030), by powering it with my new old Lambda linear power |
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88 | supply. Applying power at the leads of C1025, I could also check the |
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89 | behavior of the Q1020/Q1021 stage. Their purpose is to regulate the |
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90 | supply voltage for the U1030 main oscillator. |
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91 | |
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92 | .. image:: {static}/images/tek2445/psu_prereg_test.jpg |
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93 | :alt: Testing the main control oscillator. |
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94 | |
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95 | At power-up time, when the oscillator has not yet started, R1020 fill |
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96 | C1025 from the input high voltage DC. When the voltage on C1025 |
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97 | reaches about 21V, Q1021 is activated, powering U1030 (from C1025), |
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98 | and doing so, putting R1024 in parallel with R1020, making the voltage |
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99 | required to keep Q1021 saturated much lower (around 8V theorically). |
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100 | |
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101 | With the energy stored in C1025, U1030 can start oscillating, starting |
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102 | effecively the preregulated power supply, which make switching current |
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103 | flow through T1050, from which the coil at leads 6 and 7 should now |
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104 | provide something like the 15V used to power the main preregulator |
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105 | oscillator. So far so good. On my PSU, this main oscillator seems to |
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106 | work fine even if I've found that the voltages at which thing happen |
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107 | are significantly smaller than the values above (which come from the |
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108 | service manual). It's more like: |
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109 | |
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110 | - 18V for Q1021 to be saturated (instead of 21V), |
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111 | - 7V for Q1021 to be blocked again (instead of 8V). |
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112 | |
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113 | Not sure whether I should care about this. Probably not. |
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114 | |
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115 | The other part of the preregulator is the inverter drive. Its purpose |
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116 | is to switch the current flowing in the T1060 transformer (the output |
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117 | of the preregulator part) from one direction to the other in its |
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118 | primary circuit at each pulse of the switching in T1050. |
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119 | |
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120 | With Q1060 and Q1070 being dead, I was expecting a few more components |
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121 | around to have suffer. And some more dead puppies there were: R1060 |
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122 | and R1070 have died also (open) and, more annoying, U1066. It's a bit |
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123 | more annoying since this chip is a DS0026CN, which is obsolete and |
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124 | cannot be found at DigiKey or Mouser any more. |
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125 | |
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126 | Thanksfully, it's still available on ebay. So I've bough a pair of |
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127 | them, and that's where I am now in this epic attempt to repair this |
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128 | poor PSU. |
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129 | |
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130 | I've also bought a Rigol DS1054Z (waiting for it to be delivered |
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131 | also), I hope it will help me figure what's really going wrong in this |
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132 | preregulator stage. Obviously there is something not working properly, |
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133 | probably a high frequency signal in the switching. The creepy noise in |
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134 | T1050 and R1071 beginning to burn are clear signs of this high |
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135 | frequency noise, probably inducing high voltage spikes or some stuff |
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136 | like that. |
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137 | |
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138 | |
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139 | A few things I've noticed that seems rather strange to me: |
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140 | |
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141 | - R1069 is marked as 100kΩ on the service manual, it was 33kΩ on mine, |
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142 | |
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143 | - the schematic indicate a +264V at the output of the T1020 choke, but |
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144 | I don't understand how such a low value is possible (with a 240VAC |
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145 | input voltage, I expect this value to be around 330V, which is the |
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146 | value I measured IIRC), |
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147 | |
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148 | - voltage values indicated on the schematic in the service manual with |
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149 | a * sign should be with respect to REF signal. But I don't see how |
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150 | the voltage at the terminals of U1030 can be given relative to |
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151 | REF. I read (and measured) these values realted to the GND pins of |
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152 | U1030, which is the switched +264V (or +330V in my case) high |
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153 | voltage at the middle terminal of the primary coil of the output |
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154 | transformer. |
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155 | |
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156 | While waiting for my DS0026 spare ICs, I'm trying to figure how I can |
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157 | elaborate a setup in which I am able to test the PSU without risking |
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158 | its life again. I'll have to find my variac in my cellar, I guess. |
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159 |